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LATEST UPDATE OF THIS PAGE: 4/15/06
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Replacing an
Upright Piano Pinblock
The
project described below was recently completed on an 1888 Everett
Upright piano. The original pinblock was seriously defective,
especially in the treble section: about half the pins had
insufficient torque to hold the strings at concert pitch. Clearly,
the pinblock needed to be replaced. Our clients had a strong
attraction to this beautiful vintage piano, and they were willing to
invest in having this major improvement completed. We also
reconditioned the action of this piano, and we were confident that
the outcome would be a fine musical instrument.
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1 –
Softening and cracking of the pinblock has resulted in the tuning
pins being too loose to sustain pitch. We will need to make and
install a new pinblock. |

2 –
We
dismantled the piano, removing the
action, the keybed, the pedal board, the back of the lid, the
strings and the plate--leaving the soundboard and pinblock exposed. |
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3 –
We carefully marked the locations of all holes in the pinblock, the upper bridges, and the 1/4"-thick bass pinblock
cap. |

4
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The main tool for removing the
pinblock is a 3/8" drill bit 18 inches long, and a special jig
designed by Andrew Bolduc of Quebec, Canada. |
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5 – With our
skill-saw, we cut two grooves 2" deep into the pinblock,
just above the glue-joint, leaving a "guide hole" the same width as
the drill bit. Then we used the Bolduc Pinblock Extractor Jig to
drill a series of parallel holes through the pinblock, extending just
above the soundboard. |

6 –
For drilling the
last four holes just inside the sidewalls, we disassembled the jig
and reassembled it using only the right or left two screws. This
enabled us to cut into the pinblock right up to each sidewall. |
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7
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We drilled a series of vertical
holes through the pinblock at each end. . . |

8 –
. . . and we cut through the pinblock with our skill saw at each end as close as
possible to the sidewalls. |
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9
– Finally, we cut through the pinblock just above the soundboard,
being sure not to cut into the soundboard material. |

10 –
We pried the main section
of the pinblock upward with long screwdrivers and a crowbar, leaving the lower half of each drill hole in
the piano. |
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11
– Using hot water, a steam
iron, and chisels, we carefully loosened the glue joint under the
remaining thin layer of the old pinblock. |

12 –
We cleaned the surfaces on
which the old pinblock had been installed, preparing a flat surface
for installing the
replacement pinblock. |
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13
–
We repaired the soundboard and refinished
it with sealer and spar urethane. |

14
– After cleaning the plate and the plate pins, we re-installed the
plate in
the piano, placing all bolts in the original locations. |
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15 –
We cut a piece of new pinblock
material to fit precisely between the two sidewalls and then fit the
lower edge to the upper edge of the plate. |

16
– Using the mylar pattern to plot exact locations, we installed a
new 1/4" cap in the bass area, and we drilled eight holes: for the
action bolts and for the large pinblock bolts. Before drilling
tuning pin holes, we refinished the new pinblock with three coats of
sealer, rubbed down with extra fine sandpaper and steel wool. |
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17 –
After taping the mylar in place and positioning the upper treble
bridge, we punched tuning pin-size holes through the mylar template,
marked the holes, and enlarged the centers with a countersink bit. |

18 –
We followed the same process in the bass section of the pinblock. |
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19 –
We drilled the
tuning pin holes with a .251 bit at a 6-degree angle, and with a
compressed air-blower attached to the drill to remove wood and cool
the bit during drilling. |

20 –
Using the pressure bar as a template, we drilled screw-starter holes
through the upper bridge into the pinblock, and we dry-fitted the
pressure bar. |
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21 –
We
installed new bridge pins on the
upper bass bridge. |

22 –
After spreading a thick layer of glue on the "pinblock bed" and
inner sidewalls of the piano, we clamped and bolted the new pinblock
in place, letting the glue dry overnight. |
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23
– Next
morning, we removed the clamps, and we installed new understring
felt. |

24
–
After restringing, we installed the
pressure bar over the treble section and positioned it to press down
on the strings at the depth required for keeping the strings in
place. Project completed! Now, to action
reconditioning. . . |
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